NATIONAL
TRANSPORTATION
SAFETY BOARD
WASHINGTON, D.C. 20594
RAILROAD ACCIDENT REPORT
PB2002-916302
NTSB/RAR-02/02
Derailment of CSX Transportation Coal Train V986-26
at Bloomington, Maryland, January 30, 2000
7445
THE CORRECTIONS BELOW ARE INCLUDED
IN THIS VERSION OF THE PUBLISHED REPORT
RAILROAD ACCIDENT REPORT
NTSB/RAR-02/02 (PB2002-916302)
DERAILMENT OF CSX TRANSPORTATION COAL TRAIN V986-26
AT BLOOMINGTON, MARYLAND
January 30, 2000
Page 24 has been updated with the correct junction name. (12 Aug 2002)
The name originally printed as Virginia Central Junction.
Page 20 has been updated to correct the data in Table 2 under the column heading Coefficient of Friction for
Car Type, CSXT 392663, Step 13. (21 May 2003)
The data originally printed as 03263.
Railroad Accident Report
Derailment of CSX Transportation Coal Train V986-26
at Bloomington, Maryland, January 30, 2000
NTSB/RAR-02/02
PB2002-916302 National Transportation Safety Board
Notation 7445 490 L’Enfant Plaza, S.W.
Adopted March 5, 2002 Washington, D.C. 20594
National Transportation Safety Board. 2002. Derailment of CSX Transportation Coal Train V986-26
at Bloomington, Maryland, January 30, 2000. Railroad Accident Report NTSB/RAR-02/02.
Washington, DC.
Abstract: About 7:00 a.m. on January 30, 2000, eastbound loaded CSX Transportation coal train V986-26
lost effective braking while descending a section of track known as “17-mile grade” from Altamont to
Bloomington, Maryland, and derailed 76 of its 80 “bathtub” high-side gondola cars when the train failed to
negotiate curves at excessive speed. The derailed cars destroyed a nearby occupied residence, killing a 15-
year-old boy and seriously injuring his mother. Three other occupants of the residence escaped with little
or no injury. Track and equipment damages were estimated to be in excess of $3.2 million. There was no
resulting fire or hazardous materials release.
The safety issues addressed in the report include the determination and designation of maximum
authorized train speeds with sufficient safety margins to ensure that a train can be stopped by the air brake
system alone; locomotive engineer support and training; and engineer knowledge of the condition of the
dynamic braking system before and during use.
As a result of its investigation of this accident, the Safety Board makes safety recommendations to CSX
Transportation and all class I railroads.
The National Transportation Safety Board is an independent Federal agency dedicated to promoting aviation, railroad, highway, marine,
pipeline, and hazardous materials safety. Established in 1967, the agency is mandated by Congress through the Independent Safety Board
Act of 1974 to investigate transportation accidents, determine the probable causes of the accidents, issue safety recommendations, study
transportation safety issues, and evaluate the safety effectiveness of government agencies involved in transportation. The Safety Board
makes public its actions and decisions through accident reports, safety studies, special investigation reports, safety recommendations, and
statistical reviews.
Recent publications are available in their entirety on the Web at <http://www.ntsb.gov>. Other information about available publications also
may be obtained from the Web site or by contacting:
National Transportation Safety Board
Public Inquiries Section, RE-51
490 L’Enfant Plaza, S.W.
Washington, D.C. 20594
(800) 877-6799 or (202) 314-6551
Safety Board publications may be purchased, by individual copy or by subscription, from the National Technical Information Service. To
purchase this publication, order report number PB2002-916302 from:
National Technical Information Service
5285 Port Royal Road
Springfield, Virginia 22161
(800) 553-6847 or (703) 605-6000
The Independent Safety Board Act, as codified at 49 U.S.C. Section 1154(b), precludes the admission into evidence or use of Board reports
related to an incident or accident in a civil action for damages resulting from a matter mentioned in the report.
iii Railroad Accident Report
Contents
Executive Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv
Factual Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
Accident Synopsis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
Accident Narrative . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2
Train Makeup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2
Train Movement . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4
Descent of 17-Mile Grade . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
Damages . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
Injuries . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10
Personnel Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
Engineer . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
Conductor . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .12
Trainman Trainee . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
Train Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
Train Equipment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12
Track Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
Signal Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
Operations Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
Meteorological Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
Toxicological Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
Tests and Research . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
Track and Signal Tests . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
Accident Site Inspection of Cars . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
End-of-Train Test . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
Locomotive Tests and Inspections . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
Multiple-Unit Cable . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
Event Recorders . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
Calculation of Braking Horsepower . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17
Load Cell Brake Shoe Test . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18
Dynamometer Tests . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19
Other Information . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
Engineer Training . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
Determination of Maximum Authorized Speeds and Braking Capability . . . . . . . . . . 23
CSXT Postaccident Actions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
Analysis . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
Exclusions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
Weather . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
Fatigue . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
Toxicology . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 25
Track and Signals . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
Event Recorder . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
Air Brake System . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26
Dynamic Braking and Train Speed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
Contents iv Railroad Accident Report
Tread Brakes/Air Brakes and Stopping Ability . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29
CSXT Management Oversight . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
Engineer’s Actions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31
Engineer’s Support and Training . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33
Use of End-of-Train Emergency Switch . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34
Emergency Radio Use . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34
Conclusions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
Probable Cause . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 36
Recommendations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 37
Appendixes
A: Investigation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 39
B:
How Freight Train Air Brakes Work . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 41
v Railroad Accident Report
Executive Summary
About 7:00 a.m. on January 30, 2000, eastbound loaded CSX Transportation
(CSXT) coal train V986-26 lost effective braking while descending a section of track
known as “17-mile grade” from Altamont to Bloomington, Maryland, and derailed 76 of
its 80 “bathtub” high-side gondola cars when the train failed to negotiate curves at
excessive speed. The derailed cars destroyed a nearby occupied residence, killing a 15-
year-old boy and seriously injuring his mother. Three other occupants of the residence
escaped with little or no injury. Track and equipment damages were estimated to be in
excess of $3.2 million. There was no resulting fire or hazardous materials release.
The National Transportation Safety Board determines that the probable cause of
the January 30, 2000, derailment of CSX Transportation train V986-26 near Bloomington,
Maryland, was the railroad’s practice of including dynamic braking in determining
maximum authorized speed without providing the engineer with real-time information on
the status of the dynamic braking system.
The safety issues addressed in the report include:
The determination and designation of maximum authorized train speeds with
sufficient safety margins to ensure that a train can be stopped by the air brake
system alone.
Locomotive engineer support and training.
Engineer knowledge of the condition of the dynamic braking system before
and during use.
As a result of its investigation of this accident, the Safety Board makes safety
recommendations to CSX Transportation and all class I railroads.
this page intentionally left blank
1 Railroad Accident Report
Factual Information
Accident Synopsis
About 7:00 a.m. on January 30, 2000, eastbound loaded CSX Transportation
(CSXT) coal train V986-26 lost effective braking while descending a section of track
known as “17-mile grade”
1
from Altamont to Bloomington, Maryland, (figure 1) and
derailed 76 of its 80 “bathtub”
2
high-side gondola cars when the train failed to negotiate
curves at excessive speed. The derailed cars destroyed a nearby occupied residence,
killing a 15-year-old boy and seriously injuring his mother. Three other occupants of the
residence escaped with little or no injury. Track and equipment damages were estimated to
be in excess of $3.2 million. There was no resulting fire or hazardous materials release.
1
Grade is defined as the change in elevation along the track. It is expressed in percentage representing
the change in vertical elevation, in feet, over a distance of 100 feet. For example, a change in elevation of 1
foot over a distance of 100 feet would represent at 1-percent grade. Mountain, heavy, or steep grade for a
train of 4,000 trailing tons or less is a grade of 2 percent or more for a distance of 2 or more miles. For a train
with a trailing tonnage of more than 4,000 tons, steep grade is an average of 1 percent or more grade for 3 or
more miles.
2
Unlike hopper cars, these cars do not have bottom outlets and must be unloaded in a rotary dump
cradle.
Figure 1. Accident location.
Pe
n
n
sy
lvan
ia
V
irg
in
ia
W
e
st
Virgin
ia
O
h
io
MD
Bloomington
Factual Information 2 Railroad Accident Report
Accident Narrative
3
Train Makeup
CSXT train V986-26 originated at the CSXT Grafton Yard in Grafton, West
Virginia, and was destined for the Potomac Electric Power Company’s Bennings power
plant in Washington, D.C. The 80 loaded coal cars of the accident train originated at the
Sentinel (coal) Mine, which is about 13 miles from Grafton on the CSXT Cowen
Subdivision.
On January 28, 2000, a CSXT train crew put together the two previously
assembled blocks of 40 loaded coal cars that would become the accident train using a two-
locomotive consist. After the initial terminal air brake tests and equipment inspection, the
train departed the mine. At that time, the train’s brake pipe
4
air pressure was set for 90
pounds per square inch (psi), and according to the crew, the end-of-train device (EOT)
5
was showing a train line pressure of 88 1/2 psi at the rear of the train. (See appendix B for
more detailed information on the operation of freight train air brakes.) According to the
mine train crew, the movement from the mine to Grafton Yard was routine and without
incident.
When the train reached Grafton Yard, it was moved to the East Yard No. 3 track.
The locomotives were removed, and the train line was connected to an 80-psi yard air
supply to maintain brake pipe pressure.
About 11:30 p.m. on January 29, a yard crew at Grafton Yard, under the direction
of the dispatcher, assembled the three-locomotive consist of the accident train,
6
with a
former Conrail locomotive as the lead unit. (See figure 2.) Once the locomotive units were
coupled together on the eastbound track, the yard crewmembers connected the
locomotives’ air hoses and multiple-unit cables,
7
and performed an air test. They then
coupled the locomotive consist to the 80 loaded coal cars on No. 3 track that would make
up train V986-26. According to the CSXT Locomotive and Train Air Brake Test
Certificate signed by the yard crew engineer, a locomotive brake test was completed at
12:01 a.m., January 30. A successful set-and-release train brake test was also performed.
3
The following narrative is based on witness interviews as corroborated by CSXT records, official
documents, and train event recorder data.
4
Commonly called a “train line,” the brake pipe is the pipe, hose, connections, angle cocks, cut-out
cocks, fittings, etc., connecting the locomotive and all cars from one end of the train to the other for the
passage of air to charge and control the brakes.
5
An EOT transmits to the lead unit (head-end locomotive) the brake pipe pressure at the rear of the
train. Brake pipe pressure can also be seen on a digital readout on the flashing rear-end device itself.
6
The number of locomotive units assigned to eastbound coal trains had recently been increased from
two to three to preclude delays due to insufficient power.
7
The multiple-unit cable electronically connects coupled individual locomotive units, enabling them
to be controlled from one cab as one locomotive.
Factual Information 3 Railroad Accident Report
After the locomotives were attached to the accident train, a utility employee
8
removed the yard air. The yard crewmembers were instructed to move the accident train
down track No. 3 to the scale house, where they secured the train and were relieved.
The accident train crewmembers (an engineer, a conductor, and a trainman trainee)
arrived at Grafton about 2 hours later, at 2:00 a.m. on January 30. After receiving their
orders and conducting a job briefing, the accident train crewmembers went to the train.
The utility employee helped the accident engineer test the air brakes, as required by the
Federal Railroad Administration (FRA). The train line pressure was set for 90 psi, and
according to both the engineer and the utility employee, the EOT indicated a pressure of
81 psi at the rear of the train.
9
The engineer and the utility employee also successfully
tested the EOT emergency brake application feature.
10
The crew then checked that the
locomotive hand brakes were off and that the control console of each trailing locomotive
unit was set up in the proper configuration. About 2:30 a.m., the train, upon receiving the
signal from the dispatcher, departed Grafton Yard.
Figure 2. Accident locomotive consist.
8
The utility employee performs several jobs in the yard, combining functions of a brakeman, a
switchman, and a carman.
9
That the flashing rear-end device showed a brake pipe pressure of 81 pounds was later verified by the
event recorder, which recorded both the head-end and rear-end train line pressures.
10
This was a two-way EOT, which gives the engineer the capability to remotely initiate an emergency
brake application (by immediately releasing all air pressure from the train line) from the rear end of the train,
either to get a quicker application or because a train line blockage is preventing the propagation of an
application from the locomotive.
Factual Information 4 Railroad Accident Report
The utility employee said that he observed the last 30 to 35 cars of the train as it
departed and that he noted no problems. He also said that he saw no snow or ice around
the brake shoes or trucks.
Train Movement
When the train reached Newburg at milepost (MP) 267.2, it stopped so a helper
11
could be added. The engineer said that up to that point, he had not needed to use either the
air brakes or the dynamic brakes
12
to control the train.
When the helper arrived and was coupled onto the rear of the coal train, the helper
flagman (brakeman) disconnected the train line from the coal train EOT and connected it
to the helper.
13
The helper engineer told the train engineer that there were 82 pounds of
pressure and asked him to do a set-and-release brake test. After successful completion of
the test, the train proceeded east with a clear signal. From then on, except at Blaser (MP
258.9), until the helper was uncoupled at Terra Alta, the train engineer did not
communicate with the helper engineer except to call signals.
When the train reached the top of the hill at Blaser, the helper engineer radioed the
train crew that the air on the rear of the train was adequate to go down the hill. The train
proceeded down the hill at the authorized speed of 25 mph; however, the helper engineer
thought something was unusual:
I think we used 17 pounds of air
14
coming down the first hill. Which was kind of
[unusual]…. Generally, 10 to 11 [pounds of] air will hold a train off there…. But
[the coal train engineer] controlled the train at the speed limit….
The helper engineer said later that he did not say anything to the train engineer
about the heavier air brake application, even though he thought it was unusual, because
the train was under control and not exceeding the authorized speed.
The train reached the bottom of the grade at Rowlesburg and began the uphill
climb to Terra Alta. The train reached the top of the grade at Terra Alta without difficulty,
where it stopped to cut off the helper.
11
The helper was a two-unit locomotive placed on the rear of the train to help push the coal train up the
grade to Altamont.
12
Dynamic braking is a method of train braking in which the locomotive’s traction motors are
converted to electric generators driven by kinetic energy from the moving train. The generated electricity
flows into a resistor grid on the locomotive and is dissipated as heat. This electrical “load” on the traction
motor/generator acts to slow the motor shaft rotation, resulting in a braking action being applied to the train
wheels. Dynamic braking on the locomotives is completely independent of the air braking system on the
cars themselves.
13
This type of two-way EOT can remain in the coupler when another car or locomotive is coupled to it.
14
Meaning that the train line pressure was reduced by 17 psi. Brake application is modulated by the
amount of air pressure reduction. In an emergency brake application, the air pressure is quickly reduced to
zero.
Factual Information 5 Railroad Accident Report
As the train draped the crest of the grade at Terra Alta, the helper was uncoupled.
The helper brakeman reconnected the flashing EOT to the train line, but the EOT would
not register train line pressure. The helper brakeman replaced the EOT with a spare unit
carried aboard the helper, and he and the train engineer were then able to establish
telemetry and successfully performed an air test and an EOT emergency feature test.
About 5:43 a.m., the train continued east, and the helper returned to Rowlesburg.
The portion of railroad from Terra Alta to Altamont was undulating over 18.6
miles, and the maximum authorized speed for coal trains was 30 mph.
15
The eastbound
route had a brief down grade, from Terra Alta to Snowy Creek, during which the engineer
maintained a speed of 28 to 29 mph by using dynamic braking and a short and limited
application of the air brakes.
16
The engineer then went to full throttle (throttle control in
the 8th notch) and ascended the grade to Edgewood, east of the Maryland State line. Then
he descended the shallow down grade to Skipnish Fill, while he again made a short, 1-
minute, minimum 8-pound application of the air brakes, supplemented by dynamic
braking. (The engineer was unaware that the lead locomotive was the only unit on which
dynamic braking was actually being applied because of a defective multiple-unit cable
connecting the lead locomotive with the first trailing unit.) After that, the grade dropped
off rather sharply down into the Youghcogheny River Valley through Macking’s Hollow,
just west of Oakland, Maryland. The engineer used a brief minimum brake application of
10 pounds for about a minute and a half while continuously using heavy dynamic braking.
The railroad was relatively level through Oakland and then gently ascended to Mountain
Lake Park, where the grade increased and the railroad climbed up through Deer Park,
Maryland, about 2.8 miles from the grade at Altamont.
When the train reached Oakland, the engineer came out of dynamic braking and
increased the throttle, eventually accelerating to 40 mph in order to build enough
momentum to ascend to Altamont. He maintained maximum throttle (notch 8) on the
climb to Altamont, but the speed slowly dropped to 15 mph as the lead locomotive unit
crossed the summit, about 6:22 a.m. About a minute later, the speed dropped to 13 mph,
and the engineer made a minimum brake application while in throttle notch 7. He
proceeded to drag the train over the crest of the Altamont summit
17
while progressively
reducing the throttle as more of the train crested and began the descent. During this time,
the train’s speed dropped to 9 mph and then climbed to 13 mph.
Descent of 17-Mile Grade
As it began its descent at Altamont, down 17-mile grade, the train had been
running for more than 4 hours and had traveled about 58 miles. Until the train had reached
Newburg, where the helper was added, the engineer had not used either the air brakes or
15
All braking and speed information in this section is taken from locomotive event recorder data
downloaded after the accident.
16
The engineer made a 9-psi reduction of the brake pipe for about a minute over about 1/2 mile
between MPs 239.5 and 239.
17
The summit of the grade at Altamont is 2,629 feet above sea level and is crossed at that point by
Maryland Route 135.
Factual Information 6 Railroad Accident Report
the dynamic brakes. Between Newburg and Altamont (about 25 miles), the engineer made
four applications of the air brakes, totaling 43 minutes and 18 miles. One of the four
applications was the 17-pound reduction at Blaser that was noted by the helper engineer.
The train started down 17-mile grade (an average grade of 2.4 percent
18
) at 13 mph
in throttle notch 7 with a 6-pound reduction
19
of the train line. The maximum authorized
speed from Altamont to Swanton Flats was 30 mph. Over the next 3 minutes, as more of
the train crested the summit and began to descend, the engineer increased the train line
reduction to 10 psi, which increased the brake application. During this time, he also went
from pulling (throttle) to dynamic braking, which he increased to the near maximum
according to the event recorder on the lead locomotive unit. For the next 7 minutes, he
maintained heavy dynamic braking (which was affecting only the lead locomotive because
of the defective cable) and continued to increase air braking by making incremental 1-
pound reductions in train line pressure about every 30 seconds until he had a 17-pound
reduction.
About 10 minutes down the grade from Altamont, near “Swanton Flats” (Swanton
Road MP 219.4), the engineer deactivated dynamic braking and began to apply traction
power while still maintaining a 17-pound reduction in train line pressure. The maximum
authorized speed from Swanton Flats to Bloomington was 25 mph. The engineer then
powered against the train brakes for about the next 2 miles (5 minutes) while keeping the
speed between 21 and 24 mph.
When asked later if the reason he powered against the brakes was that he was
afraid of stalling out at Swanton Flats, the engineer stated, “Yes, sir. A lot of times, your
trains will hang up there if you don’t keep your speed up.” The engineer outlined the
consequences of stalling out at Swanton Flats:
You stop and then the brakeman goes back and sets up all the brakes. And then
you recharge your train and then put the air on and he’ll knock them off and then
you can continue down the hill. [This takes] I’d say a good two and a half hours
somewhere. And in that point, probably longer with the ice, the way the weather
was climbing up and down.
18
Gravity acts on each ton of train weight with a force of about 20 pounds for each percent of grade.
19
According to the engineer, he considered the reduction a “minimum” or preliminary application of
the brakes.
Factual Information 7 Railroad Accident Report
According to CSXT Train Handling Rules
20
:
When necessary to apply power descending long heavy grades, trains must not be
pulled for a distance greater than 2 miles if the brake pipe reduction is 18 pounds
[psi] or greater.
According to FRA inspectors who have ridden trains down 17-mile grade and to
CSXT operating officers and CSXT engineers who regularly operate trains through the
accident area, it is possible to control a loaded coal train headed by three modern
locomotive units with a 12-pound or less brake pipe reduction and light throttle or
dynamic brake modulation. The accident engineer stated several times that he attributed
his use of more air brake than usual to the wet snow and icy rail.
About 16 minutes down 17-mile grade, near MP 218, the engineer went from
power to heavy dynamic braking with the 17-pound reduction still applied. The train was
moving at 24 mph. Several minutes after reaching full or near-full dynamic braking (on
the lead unit only), the train’s speed reached 28 mph, and the engineer increased the train
line reduction to 18 pounds. Over the next 2 minutes, he steadily increased the train line
reduction to 26 pounds, or “full service,” in response to the train’s steadily increasing
speed.
The train failed to slow, and about 30 seconds later, while moving at 34 mph at MP
214.34, the engineer put the train brakes in “emergency,”
21
which eliminated any effect
from the dynamic braking. The train briefly slowed to 30 mph and then began to
accelerate. Despite the emergency application of the air brakes, the train’s speed steadily
increased over the next 6 minutes to 59 mph.
When the engineer placed the train in emergency, he used the automatic brake
valve handle. He did not use the switch in the cab that would have activated an emergency
application from the two-way EOT on the rear of the train. He said that he noted the EOT
was indicating a train line pressure of 0 psi about a minute and a half after he had made the
emergency application and that he therefore felt no need to activate the switch. He said
that he was taught to activate the switch only if the emergency application did not apply
on the rear.
The conductor said that he noted on his display screen that the train line had
depleted to 0 psi and that he, therefore, knew that the emergency brake application had
propagated all the way to the end of the train.
20
Effective January 1, 1998, and revised July 1, 1999, Rule 3.3.7, “Speed Control on Descending
Grade,” paragraph C: “Use of Power on Heavy Descending Grades.”
21
Emergency braking increases the brake shoe pressure on the wheel by about 25 percent over that of
full service.
Factual Information 8 Railroad Accident Report
When it became apparent that the train was uncontrollable, the engineer attempted
to radio the dispatcher on the locomotive radio but was unable to do so. According to the
engineer:
I could not contact the dispatcher. I tried the emergency button, the code 9
and applied on channel 14, but [this was] a Conrail radio, and evidently
they’re not compatible with ours [CSXT].
The conductor said:
We tried to contact the dispatcher with the engine radio, but the engine radio is a
Conrail radio, and it will not contact our dispatchers, the equipment is not
compatible. Radios are locked-in and not changeable by crews.
The trainman trainee was in the second locomotive unit cab. He said:
The first suspicion I had that anything was amiss was that the brake shoes were
burning and there was acrid smoke coming into the…cabin of the second
locomotive. I opened the window, and it was even worse. I shut it quickly. Five
minutes later, the engineer came on the radio, and said, ‘Go to channel 14 and get
the dispatcher on the radio.’ He said there was a button that I should press, number
5. Well, the second radio is different from what he had, and I didn’t know how to
operate it, so I went to channel 14, but I was still on channel 8. I broadcast the
emergency, but I was unable to get the dispatcher.
During postaccident interviews, the trainman trainee was asked if he had been
trained in making an emergency radio transmission. He said:
Yes, but getting the dispatcher on the radio here is something different. You have
to press certain buttons and I wasn’t still surehe gave me some instructions over
the radio, but the second radio was different from his, and it had no key pad, so I
did not know how to operate the second radio.
The trainman trainee stated that he had seen as many as five different styles of
radios on various locomotives but that the instructions he had been given on their use were
generic and were not specific to any particular type of radio.
Near Bond, MP 212.6, the trainman trainee inadvertently contacted the operator at
West Keyser. The operator responded and said that the train was “lit up,” or cleared for
continued movement. The conductor told the operator that the train was going through Big
Curve at 50 mph and was in “real trouble.” The conductor told the engineer that he did not
believe the train would get to the bottom of the hill at all. The conductor said that he and
the engineer discussed jumping but “figured we were going to land in a ditch someplace
with the engine on top of us. I figured our chance of survival was about zero.”
The train ultimately reached a speed of 59 mph. The train broke apart and derailed
at curves in three separate segments, starting from the rear end. At MP 210.6, the first
group of 20 cars separated, and 17 of the 20 cars derailed. At MP 209.8, another 18 cars
separated and derailed. Finally, at MP 208.2, the remaining 42 cars separated, and 41 of
Factual Information 9 Railroad Accident Report
the 42 derailed in a general pileup. (See figure 3.) Some of the 41 derailed cars struck a
nearby occupied residence, destroying the house and killing a 15-year-old boy and
seriously injuring his mother. (See figure 4.) Three other occupants of the house escaped
with minor or no injuries. Some of the 41 cars also broke a gas pipeline inside a transfer
building near the track; as a result, about 101 customers of Columbia Gas of Maryland
temporarily lost natural gas service.
Figure 3. Pileup of derailed coal cars.
Figure 4. Destroyed residence where one fatal and one serious injury occurred.
Factual Information 10 Railroad Accident Report
The three locomotive units finally came to rest more than 2 miles down the track,
at MP 206.5, just west of Piedmont Road Crossing, where the crew was subsequently
picked up and taken to Cumberland for toxicology testing and interviews.
Damages
Damages to railroad equipment totaled about $1.8 million (67 of the 76 cars that
derailed had to be scrapped). Other damages included:
Lading of coal: $182,753
Track and signal: $275,000
Private property: $288,963
Clean up: $14,297
Total damages were in excess of $3.2 million.
Injuries
Table 1. Injuries.
Injury Scale
a
CSXT Operating
Crew
Residents Total
Fatal 0 1 1
Serious 0 1 1
Minor 0 2 2
None 3 1 4
Tota l 3 5 8
a
49 Code of Federal Regulations 830.2 defines fatal injury as “any injury which results in death within 30 days of the
accident” and serious injury as “an injury which: (1) requires hospitalization for more than 48 hours, commencing within
7 days from the date the injury was received; (2) results in a fracture of any bone (except simple fractures of fingers,
toes, or nose); (3) causes severe hemorrhages, nerve, or tendon damage; (4) involves any internal organ; or (5)
involves second or third-degree burns, or any burn affecting more than 5 percent of the body surface.”
Factual Information 11 Railroad Accident Report
Personnel Information
Engineer
The Baltimore & Ohio Railroad, a CSXT predecessor, had hired the engineer in
1970. He had started in the maintenance-of-way department working on track and then
moved to the mechanical department, repairing cars and locomotives. He changed jobs
again to work in train service as a brakeman and finally went to engine service, becoming
an engineer in 1976.
According to CSXT records, the engineer had neither medical restrictions nor
disciplinary actions. His personal record file showed he had taken or received the
following required examinations, classes, tests, and certifications
22
:
Last medical examination 5-03-99
Drivers License (WV) 6-29-99
Rules Class 1-27-00 Scored 94 out of 100
FRA Locomotive Engineer Certification
23
Knowledge 5-04-99 Scored 98 out of 100
Performance 3-21-99 Scored 90 out of 100
Certified 12-31-99
Skill Performance Evaluations by a road foreman or supervisor
1-17-00 Scored 95 out of 100
6-27-98 Scored 95 out of 100
5-12-98 Scored 95 out of 100
5-11-98 Scored 90 out of 100
3-05-98 Scored 90 out of 100
9-17-97 Scored 90 out of 100
6-18-97 Scored 95 out of 100
6-13-96 Scored 95 out of 100
22
A more complete description of the evaluations and examinations can be found later in this report in
the “Evaluations” portion the “Engineer Training” section.
23
CSXT locomotive engineers are tested for FRA certification every 3 years according to 49 CFR Part
240. The FRA locomotive engineer certification program began in January 1992.
Factual Information 12 Railroad Accident Report
The engineer was considered to be one of the most senior and experienced
engineers in the Grafton area. He said that he had taken trains from Grafton to
Cumberland “thousands of times” since becoming an engineer in 1976. Before the
accident, he had been in yard service for approximately 4 years. His yard service involved
switching cars within the yard at Grafton, taking empty coal trains up to coal mines around
Grafton, and returning with loaded coal trains down grade to Grafton. He had returned to
road service on January 9 and had made a total of 20 trips, 12 westbound and 8 eastbound,
between Grafton and Cumberland before the accident. Of the eight eastbound trips, all but
one were with loaded coal trains.
The engineer made a trip on January 29, the day before the accident. According to
CSXT computer records, he was relieved at 11:00 a.m. and off at 12:15 p.m.
24
He said he
went home and ate and was asleep by about 2:30 p.m. At 9:30 p.m., about 7 hours later, he
said, he was called to report at 11:30 p.m. for the accident train.
25
He said he reported to
the Cumberland Yard office about 11:30 p.m. He and the crew were then sent by taxi to
Grafton, where they arrived about 2:00 a.m. on January 30. He said he felt well rested
when he came on duty.
Conductor
The conductor stated that he had been off for 11 hours and 30 minutes before
reporting for the accident train. He was not a qualified engineer.
Trainman Trainee
The trainman trainee had been on the railroad for about a month before the
accident. He had spent most of the time in a classroom in Atlanta, Georgia, taking part of
his CSXT initial training. He had had no previous railroad experience. At the time of the
accident, he was sitting in the second locomotive unit cab because the engineer smoked
and he did not like the cigarette smoke.
Train Information
Train Equipment
The locomotive for the accident train consisted of three locomotive units; CSXT
806 (an ex-Conrail unit) was lead, BNSF
26
9481 trailed next, and CSXT 8666 was last.
General Motors Electromotive Division manufactured all the locomotive units, which
were high-horsepower six-axle locomotive units with high-adhesion trucks and extended
range dynamic braking capability.
24
Eastbound loaded coal train V986-28. On-duty time was 11:30 p.m. on January 29.
25
The engineer was off 11 hours and 15 minutes between the time he finished and 11:30 p.m., the time
he was to report.
26
Burlington Northern Santa Fe Railway.
Factual Information 13 Railroad Accident Report
The first unit, CSXT 806, was an SD80MAC; BNSF 9481 was an SD70MAC; and
CSXT 8666 was an SD50. On these units, maximum dynamic braking is achieved when
the locomotive is traveling between 4 and 24 mph. The maximum dynamic braking effort
is 96,000 pounds for an SD80MAC, 81,000 pounds for an SD70MAC, and 60,000 pounds
for an SD50.
The accident train had 80 coal cars, all of which were high-side “bathtub” gondola
cars designed for unit coal train service. The cars were relatively uniform in appearance.
Each car was 45 feet long (48 feet, 8 inches long over the couplers) and had two two-axle
trucks and 36-inch wheels. The cars were used between coalmines and power plants. The
cars had been inspected and repaired as necessary at CSXT facilities at either Curtis Bay
or Brunswick, Maryland.
According to the CSXT consist list, the train was 4,145 feet long (the length of the
combined cars was 3,920 feet). The trailing tonnage (the cars only) was 10,569 tons, and
the tons per operative brake
27
was 132.
Track Information
The railroad from Grafton to Cumberland, Maryland, which traverses the accident
area, was built about 150 years ago as part of the Baltimore and Ohio Railroad.
28
The
general east-west railroad line location and grade have remained unchanged. The railroad
is now part of CSXT Allegheny Division (formerly the Baltimore Division), Mountain
Subdivision, and consists of two mainline tracks: No. 1 (westbound)
29
and No. 2
(eastbound), with their attendant sidings and industrial spurs. Most of the rail is
continuous welded rail with some jointed rail, which varies in size from 122 to 140
pounds,
30
depending on location. The rail was manufactured from 1951 through 1998, and
the track was last surfaced during the 1980s, when crossties were replaced. The maximum
authorized speed varies from 25 to 45 mph, depending on the location of the track and the
type of train.
The site of the accident, 17-mile grade, is the railroad between Altamont (MP
223.4) and Bloomington (MP 208.6) and has an average 2.4-percent grade. The grade has
10 rail lubricators.
31
27
Tons per operative brake is the total trailing tonnage divided by the number of freight car brake
control valves, which usually corresponds to one per car, as in this case.
28
The Baltimore and Ohio Railroad reached Wheeling, West Virginia, over this railroad on
December 24, 1852.
29
The No. 1 main track is the northernmost track.
30
Rail sizes are standardized by weight per 3-foot length by the American Railway Engineering
Association (AREA), a component of the Association of American Railroads.
31
Rail lubricators are fixed devices, usually located near railroad track curves, that lubricate the side of
the railhead to minimize rail and wheel wear.
Factual Information 14 Railroad Accident Report
Signal Information
Train movement on the two mainline tracks is governed by visual indication of
automatic block, color-position wayside signals set for movement in the above indicated
direction (No. 1 track westbound, No, 2 track eastbound) for each track only. Train
movements in the opposite direction of the set signals are made under some form of train
order authority from the dispatcher.
Operations Information
Train movements between Grafton and Cumberland were governed by the
following: wayside block signal indication; CSXT Allegheny Division Timetable No. 1,
effective January 1, 2000, for the Mountain Subdivision; and CSXT Allegheny Division
Western District General Bulletins.
According to the timetable in effect at the time of the accident, for eastbound
loaded coal trains, the maximum authorized speed between Altamont and Swanton was 30
mph; between Swanton and Bloomington (MP 208.6), the maximum authorized speed
was 25 mph.
Meteorological Information
The CSXT utility employee who worked on the accident train in Grafton stated
that the temperature was warming and that the precipitation had changed from snow to
sleet and then rain. By the time the train had left Grafton, he said, the temperature had
warmed to the mid- to high 30s and “everything was thawing out.”
The train conductor said that some freezing rain was falling in Grafton when the
crew was releasing the hand brakes. He said that the grab irons were slippery and that the
crew took extra care. He said that during the trip, it was snowing with a little bit of snow
on the cap of the rail. He also said that there was some blowing snow.
The engineer said:
The ground was covered, and it was snowing and raining and sleeting…. It was
raining when we left Grafton, and [as we traveled] further east…it turned to snow
and ice. The rails were covered with wet snow and ice. We were clearing the rail
as we went.
When asked what the temperature was at the time, he said, “approximately in the
20s.”
Investigators asked the helper brakeman whether any ice or snow had built up on
the trucks or brake shoes of the cars when the helper locomotive was attached. He said that
Factual Information 15 Railroad Accident Report
it had been snowing but that he had not noticed any ice or snow on the running gear. He
said that the snow had been 3 or 4 inches deep but that it had not been on or above the
rails.
The National Weather Service described the weather at the time of the accident as
follows:
Morgantown
0653 EST. Sky overcast; winds 170 degrees at 5 knots; visibility 10 miles;
temperature 36° F; dew point 36° F; snow ended 0630 EST.
0706 EST. Sky overcast; winds 150 degrees at 5 knots; visibility 10 miles;
temperature 36° F; dew point 36° F.
Martinsburg
0650 EST. Sky overcast; winds calm; visibility 2 miles; light snow; temperature
41° F; dew point 21° F; 4 inches of snow on the ground.
0750 EST. Sky overcast; winds 020 degrees at 4 knots; visibility 4 miles; mist;
temperature 23° F; dew point 21° F. Snow ended 0740 EST.
Petersburg
0650 EST. Sky overcast; winds calm; visibility 10 miles; temperature 27° F; dew
point 27° F.
0750 EST. Sky overcast; winds calm; visibility 10 miles; temperature 23° F; dew
point 23° F.
Toxicological Information
The engineer and conductor were taken to Memorial Hospital in Cumberland
about 2 hours after the derailment, where they gave blood and urine specimens for the
toxicological testing required by the FRA.
32
The results of the tests were negative for
drugs and alcohol.
32
49 CFR 219.201.
Factual Information 16 Railroad Accident Report
Tests and Research
Track and Signal Tests
Postaccident track inspections and a review of the maintenance-of-way records
revealed no track anomalies. The 10 rail lubricators in the accident area were inspected
and found to function as designed with no discharge of excess lubricant noted.
Postaccident tests and a review of the records indicated that the signal and train control
systems functioned as designed.
Accident Site Inspection of Cars
Safety Board investigators examined the derailed and wrecked coal cars on the day
of the accident. Because so many of the cars had been completely destroyed, a brake
function test could not be performed; however, almost all of the brake shoes and wheels
showed signs of heavy braking. Wheel treads had bluing, indicating enough heat had been
generated to change the micro-structure of the steel. Brake shoe surfaces were burned and
blackened from the oxidation and melting of the composites that make up the shoes. The
severity and consistency of the damage to the brake shoes indicated that the emergency
brake application had fully propagated through the train to the last car. That the
application had fully propagated was later substantiated by the event recorder data from
the EOT.
End-of-Train Test
The flashing EOT telemetry device on the end coupler of the last car in the train
survived the accident because the last car did not derail. On February 2, 2000, the
communications maintainer at the CSXT Cumberland radio shop tested the flashing rear-
end device. All communication and pneumatic functions performed as designed. Battery
voltage was found to be 13 volts, the proper voltage.
Locomotive Tests and Inspections
The locomotive consist for train V986-26 survived the accident intact. Safety
Board investigators found nothing in the maintenance and service records for the
locomotive units that indicated a condition that would have caused or contributed to the
accident.
Investigators measured and recorded brake shoe thickness and brake cylinder
piston travel. They compared the recorded air brake pressure readings of the equalizing
reservoir, brake pipe, brake cylinder, and main reservoir of each locomotive unit to
specifications. Other than what had been affected by the excessive wear caused by the
heavy braking during the accident, everything was within specifications and standards.
On February 1, 2000, the Cumberland locomotive shop tested the air brakes of the
locomotive consist. The brake pipe leaked 2 pounds in 3 minutes, which was within
acceptable limits. The main reservoir leaked 4 pounds in 3 minutes, which was
unacceptable. A leak was found in the main reservoir. The leak was behind the clamp in
Factual Information 17 Railroad Accident Report
front of the No. 2 main reservoir cylinder on the lead locomotive unit, CSXT 806.
Investigators determined that such a leak would not affect the application of the train or
locomotive air brakes but would lower the pressure of the main reservoir enough to cause
the air compressors to activate more frequently.
Postaccident testing of the engineers radio and subsequent investigation revealed
that the radio worked as designed.
Multiple-Unit Cable
Mechanical personnel from the Cumberland locomotive shop tested the dynamic
braking system about 1:30 p.m. on January 31 at Westernport, Maryland. The testing was
under the auspices of FRA inspectors. The No. 24 pin socket of the multiple-unit cable
between the first and second locomotive units was defective. The defect prevented the
dynamic brake excitation voltage of the lead unit from reaching the two trailing units.
Thus, only the lead unit produced dynamic braking. Testers replaced the defective
multiple-unit cable and performed both a static and running test of the dynamic brake
system of the locomotive consist. The system then worked properly.
Event Recorders
CSXT personnel downloaded the data from the event recorders of all three
locomotive units. They gave floppy diskettes containing the data files to Safety Board
investigators at the accident scene. The Safety Board’s laboratory in Washington, D.C.,
examined the diskettes. Event recorder mileposts and times were based on evidence
gathered at the accident site. Locomotives CSXT 806 (the lead) and BNSF 9481 had
Rockwell solid-state event recorders. Locomotive CSXT 8666 had a Quantum
Engineering, Inc., event recorder. The data from all three locomotive matched in all
significant parameters.
Calculation of Braking Horsepower
The air-brake system is a powered braking system that uses the power of
compressed air to move a series of rods and levers on each locomotive and car to force a
brake shoe against each wheel tread to slow or stop the rotation of the wheel by friction.
Thus the tread brakes, also called the “friction brakes,” may be considered a
subcomponent of the overall air-brake system. Since the retarding or braking force is
generated by friction, a great deal of heat is created when the brakes are applied. The
energy and resultant heat is commonly expressed as braking horsepower (bhp). The more
energy and effort that is needed to stop a train, the greater the braking horsepower, and the
greater the heat. High braking horsepower involving tread brakes is synonymous with the
creation of high heat and temperatures. Modern composition brake shoes are designed to
withstand temperatures up to about 500° F but rapidly deteriorate at higher temperatures.
After the accident, theoretical calculations were performed to determine if the
accident train speed may have exceeded the capacity of the tread-braked air-brake system
Factual Information 18 Railroad Accident Report
to stop the train, and if so, when. The calculations and method used were developed by
David G. Blaine
33
for use by air brake and brake shoe manufacturers.
34
According to the above reference, the maximum safe braking horsepower for safe
practical operation is 30 bhp for a 36-inch wheel.
35
The calculated bhp per wheel for the
accident train traveling at various speeds down a 2.4 percent grade was as follows:
Speed Braking Horsepower (bhp)
(in miles per hour) per Wheel
5 9.69
10 19.12
20 33.45
30 48.75
In order for the accident train on 17-mile grade to maintain 30 bhp or less, the
accident train would have had to travel no faster than 15 mph.
Load Cell Brake Shoe Test
In order to validate the theoretical bhp calculations, it was necessary to perform
some type of actual braking tests, either with an identical train or by using a dynamometer.
For safety reasons, arrangements were made with Wabtec (formerly Westinghouse Air
Brake) to conduct dynamometer tests.
As a prerequisite for accurate dynamometer testing, actual brake shoe force against
the wheel must be used. Actual brake shoe forces are measured on a static car using a
load-cell brake shoe device, sometimes called a “golden shoe” or “gym shoe.” The car
brake shoes are replaced with brake shoes that are embedded with pressure-sensitive
transducers.
36
When the brakes are applied, the pressure of the shoe against the wheel
changes the conductivity of the electrical circuit through the shoe, which is then converted
to a force reading and recorded.
Because all but four coal cars were destroyed or severely damaged in the
derailment, three exemplar cars, one each of the three major car types involved in the
accident,
37
were tested under the direction of the Safety Board at the CSXT car shop in
Cumberland, Maryland, on August 8 and 9, 2000. All parties to the investigation
33
See American Society of Mechanical Engineers (ASME) publication 69-WA/RR-6, “Determining
Practical Tonnage Limits and Speeds in Grade Operations,” by David G. Blaine as presented to the ASME
conference in November 1969.
34
Other referenced braking documents were “Calculated Tonnage Per Operative Brake in Grade
Service,” for the Air Brake Association Annual Meeting, September 12, 1961; and “Braking Duty in North
American Freight Train Service and Effects on Brake Equipment, Brake Shoes and Wheels,” by D.G. Blaine,
F.J. Grejda, and J.C. Kahr, January 25, 1978.
35
All the cars in the accident train had 36-inch wheels.
36
A transducer is a device that converts one form of energy into another.
37
Although four types of cars were used in the accident train consist, only three types were tested since
only five cars of the fourth type were in the train.
Factual Information 19 Railroad Accident Report
participated in the testing. Wabtec technicians from the company’s facility in Wilmerding,
Pennsylvania, were provided, along with the device to assist in the tests.
Twenty-one consecutive air brake applications
38
or “steps” were made using a cart-
mounted control valve at the same pressures and in the same sequence as those made by
the accident engineer and recorded by the accident train’s event recorders. After each
application, the brake rigging was tapped with hammers to simulate the movement and
vibration of the moving accident train, and then raw force readings were taken for each of
the eight brake shoe locations on each of the three cars. There were 168 readings for each
car, for a total of 672 separate recorded raw force measurements. The Wabtec technicians
then converted these raw force numbers into actual force readings, and a single application
reading for each car was developed by averaging the readings from the eight shoe
locations for each air brake change for each car. These readings were later used on the
dynamometer machine.
Dynamometer Tests
The Association of American Railroads (AAR) sets performance specifications for
high-friction composition-type brake shoes such as those involved in the accident and for
the manner in which such brake shoes are tested for acceptability. Specifications and
procedures can be found in the AAR Manual of Standards and Recommended Practices,
Specification M-926-99. All railroad brake shoe manufacturers are required to test their
brake shoes periodically to ensure that the shoes meet the AAR’s specifications. To ensure
compliance, the AAR periodically reviews brake shoe tests. Consequently, the brake shoe
manufacturers have dynamometer machines for testing brake shoes.
The dynamometer consists of a large electrical motor that turns a shaft on which
fixed and movable inertial discs are attached to provide momentum. At the end of the shaft
is a modified
39
railroad car wheel. When the wheel is spun, the test brake shoe is applied to
the wheel tread as it would be during the actual braking of a railroad car or locomotive.
Mounted sensors on the dynamometer are attached to a computer that calculates velocity,
net shoe force, average wheel temperature, retarding force, coefficient of friction, and bhp.
On August 22, 2000, representatives of parties to the accident gathered at the
Railroad Friction Products Corporation plant at Maxton (Laurinburg), North Carolina,
where a dynamometer machine tested brake shoes under the accident conditions. Speeds
and application times were taken from the event recorder data. The shoe forces used were
those previously measured and recorded at Cumberland for each of the three major coal
car types involved in the accident. The difference between the ambient temperature of
January, when the accident took place, and that of August was not considered significant
because of the magnitude of the temperatures that develop at the shoe-wheel interface.
Each of the new brake shoes used for the simulation was broken in or slightly worn before
38
Almost all of these applications were 1-pound incremental brake pipe reductions.
39
The dynamometer railroad car wheel has a slightly modified tread profile to allow a more accurate
measurement of the temperature, pressure, and coefficient of friction.
Factual Information 20 Railroad Accident Report
being used, following the practice in brake shoe testing that the AAR recommends in
order to provide the most realistic response.
Shoe forces, velocity (train speed), and application times were preprogrammed
into the dynamometer control computer for each of the three coal car types. The computer
then drove the dynamometer and applied the brake shoe to simulate the forces, speeds, and
timing of the accident. This procedure was followed for each type of car. The computer
then recorded the resulting wheel temperatures, retarding forces, coefficients of friction,
and horsepower values. (See table 2.)
Based on these values, for two of the three car types tested, the tests showed a loss
of retardation and braking ability under operating and braking conditions that existed
between steps 11 and 12 in table 2. For the other car type, loss of braking efficiency
occurred under the conditions existing between steps 12 and 13. These steps correspond to
the braking actions the accident engineer took when the train was between MP 220.12
(step 11) and MP 216.46 (step 12), or MP 216.34 (step 13). These locations match the area
at Swanton Flats where the engineer powered against the train air brakes (17-psi reduction
of the train line) for several miles while traveling 23 to 28 mph.
Other Information
Engineer Training
Classroom Training. CSXT began its engineer recertification program in 1992. In
2000, the program involved 2 1/2 days of classroom presentations and testing. The FRA
requires an engineer to be recertified every 3 years. CSXT requires the engineer to take the
Table 2. Braking Efficiency.
Car Type Step Milepost MPH Temp F
Force
lbs.
Coefficient
of Friction
BHP
CSXT 11 220.12 23.8 431 1013 0.434 64
392663 12 216.46 27.8 598 669 0.259 50
13 216.34 27.9 606 703 0.326 52
CSXT 11 220.12 23.9 329 829 0.433 53
385995 12 216.46 27.9 557 611 0.294 45
13 216.34 27.9 565 655 0.277 49
NYC 11 220.12 23.8 335 821 0.445 52
503250 12 216.46 27.8 536 566 0.310 42
13 216.34 27.8 542 602 0.286 45
Factual Information 21 Railroad Accident Report
recertification training and testing sometime during the third year. If the engineer
successfully completes the training, CSXT issues the certification card on the last day of
that year.
Recertification classes were held in Atlanta, Georgia, and in Cumberland, where
the accident engineer was recertified. Before he took the class, CSXT had mailed him a
workbook. He was required to fill out the workbook (by answering between 250 and 300
questions) before reporting to class. A completed workbook was a condition of class
attendance and was checked by the instructors for completeness and correctness. The
workbook questions focused on FRA-required subject matter.
The classroom instruction focused on updating the engineers on air brake methods,
new locomotives and equipment, hazardous materials, and changes in train handling rules.
Each engineer took a knowledge test, which included a customized part devoted to the
unique physical characteristics of the portion of the railroad on which the engineer
operated. The accident engineer took the classroom training in May 1999 and scored 98
out of 100 on the written examination.
Evaluations. Each engineers performance is evaluated at least once a year by
railroad operating officials, usually the road foreman. The CSXT Locomotive Engineer
Evaluation Report is the form used in the evaluation. When the evaluation is done in the
same year that the engineer is to be recertified, the evaluation also serves as the
recertification performance test, since the criteria and standards are the same. The accident
engineers last recertification performance evaluation was on March 21, 1999. He scored
90 out of 100. The evaluation was done on the Thomas Subdivision at BAH-28 while he
was in switching service. He lost 10 points because, according to the form, he “didn’t
make standing and running brake test on initial movement [and] didn’t test handbrake.”
The accident engineer was evaluated on January 17, 2000, about 2 weeks before
the accident, when a road foreman of engines evaluated him on an eastbound loaded coal
train
40
and gave him a score of 95 out of 100 points. According to the form, 6 safety rules,
17 operating rules, and crew resource management were discussed. The discussion
included efficiency tests and the downloading of event recorders. The form shows that the
road foreman rode with the accident engineer for 7 hours, from Grafton to Keyser, which
should have included the accident area. However, when the engineer was asked whether a
road foreman had ever ridden with him from Altamont down to Bloomington on 17-mile
grade before the accident,
41
he replied, “No.” He indicated that no road foreman who had
evaluated him had ever made a complete trip. He said that the road foremen rode between
Keyser and Cumberland, or between Grafton and Rowlesburg, on either side of the
accident area, but not through the accident area. CSXT presented evidence that the
engineer had made a trip down 17-mile grade on January 17, 2000, accompanied by a road
foreman and another qualified engineer, but that the qualified engineer was operating the
train, with the accident engineer observing.
40
Train U822-15 was similar to the accident train; it had 82 cars and 10,470 trailing tons.
41
For purposes other than an efficiency test.
Factual Information 22 Railroad Accident Report
As a result of the Safety Board investigation of the runaway and subsequent
derailment of a Southern Pacific Transportation Company train in San Bernardino,
California, in 1989,
42
the Safety Board issued the following recommendation to the FRA
regarding engineer qualification and supervisory oversight:
R-90-22
Promulgate regulations regarding the qualification of engineers to require that
supervisors ride with an engineer in both directions on mountain grade territory
before qualifying the engineer over the entire territory and that the ride be
performed on a train that is comparable in size and trailing tonnage to those
typically most difficult to operate on that territory.
The FRA issued regulations (49 Code of Federal Regulations [CFR] Part 240
Subpart B, and section 240.127) that fulfilled the recommendation. The recommendation
was classified “ClosedAcceptable Action” on January 21, 1992. As a result of this
recommendation, all railroads, including CSXT, now include such requirements in their
operating and engineer qualification rules.
Pilot Request. According to CSXT Rule 520:
Engineers must be fully familiar with the physical characteristics of the territory
over which they are called to operate. An engineer must not accept a call to
operate over a territory that the engineer has not been over in the previous 12
months.
Because the engineer had been in yard service for 4 years before taking this road
assignment, he requested a pilot
43
from the road foreman upon his return to road service on
January 9, 2000.
The engineer said:
I talked to the road foreman, general road foreman, and he told me that I could
have a pilot for two round trips. I got one, one trip out of Cumberland
[westbound]. We brought a train out and taxied back to Cumberland, and when I
asked for one on the second call I was told [by the crew caller] that [he] and the
lead caller would decide if I needed one.
44
If so, there would be one there, and
when I reported to work, there was none.
42
National Transportation Safety Board, Derailment of Southern Pacific Transportation Company
Freight Train on May 12, 1989, and Subsequent Rupture of Calnev Petroleum Pipeline on May 25, 1989,
San Bernardino, California, Railroad Accident Report NTSB/RAR-90/02 (Washington, D.C.: NTSB, 1989).
43
A pilot is a qualified employee assigned to a train when the engineer or conductor is not acquainted
with the rules or the portion of a railroad over which the train is to be moved.
44
Crew callers are not railroad officials or supervisors and do not have the authority to make such
determinations. The CSXT superintendent stated that the crew callers response to the engineers request
was a serious breach of policy and procedure and said that CSXT had taken steps to prevent similar
incidents.
Factual Information 23 Railroad Accident Report
The engineer said he was aware that the road foreman who normally made
arrangements for a pilot was in Richmond, Virginia, at the time and therefore was
unavailable. Consequently the engineer never had a pilot for an eastbound trip (which
included descending 17-mile grade).
Two-Way EOT Training. When asked whether he was trained to activate the two-
way EOT emergency switch after an emergency application with the brake handle, the
engineer testified that the EOT emergency switch was to be used only if the EOT was not
showing 0 psi at the rear of the train after the emergency application was made.
According to the CSXT manager of engineer training, at the time the accident
engineer took his recertification training, two-way EOTs were being introduced. He said
the procedure to activate an EOT emergency brake application along with a brake handle
emergency was taught orally but that instructional materials had not yet been updated to
document this new training. He said he believed that the accident engineer had received
this new instruction during recertification training, but he could not document the training.
After the accident, CSXT expedited the updating of instructional materials and
tests to reflect the EOT activation procedure when making a brake handle emergency
application. In addition, all new EOTs purchased by CSXT have a feature that
automatically and simultaneously initiates an emergency application at the rear of the train
when an emergency application of the brakes is made by the automatic brake handle in the
locomotive cab.
Determination of Maximum Authorized Speeds and Braking Capability
Railroads determine maximum authorized speeds for various rail segments based
on a number of factors, such as tons per operative brake for control and stopping ability,
descending grade, signal spacing, and track structure. Any one factor may be the decisive
factor in determining the maximum authorized speed. The lowest speed associated with
any one factor will usually become the maximum authorized speed.
For the past decade, most railroads, including CSXT, have also used a
computerized train dynamics analyzer machine to help determine maximum authorized
speeds and appropriate train handling procedures. The use of the train dynamics analyzer
has grown as locomotive and braking technology have advanced. According to those
familiar with the capabilities of train dynamics analyzers, the machines cannot accurately
replicate the complex phenomenon of heat fade that occurs between the brake shoes and
wheel tread under severe braking conditions.
According to the CSXT manager of accident prevention, the maximum authorized
train speed for coal trains down 17-mile grade had been 25 mph for at least the past 20
years, the period for which timetable documentation was available. The CSXT central
region vice president told Safety Board investigators that CSXT included the
supplemental braking effects of dynamic braking when the railroad determined maximum
authorized speeds for various track segments. Because dynamic braking may fail suddenly
Factual Information 24 Railroad Accident Report
and without warning, it is not considered by the FRA to be sufficiently reliable to be used
in determining maximum authorized speeds.
The FRA does not specifically set or directly monitor railroad maximum
authorized speeds, although it does regulate train braking, which is a factor in setting
maximum authorized speeds.
45
Because the air brake system is the only train braking system that can both be
operated from the locomotive and reliably stop a train,
46
that system is considered the
train’s primary braking system. This concept was not codified until after the accident in
the revised power brake regulations, Brake System Safety Standards for Freight and Other
Non-Passenger Trains and Equipment, at 49 CFR Part 232, which were issued on
January 17, 2001, and made effective in May 2001. Part 232 regulation series 100 and 200
will not become effective until April 2004. One of these regulations, Part 232.103(a),
states that:
A train’s primary brake system shall be capable of stopping the train with a
service application from its maximum operating speed within the signal spacing
existing on the track over which the train is operating.
Also, 49 CFR 232.109(j) states:
The railroad’s operating rules shall be based on the premise that the friction brakes
are sufficient by themselves, without the aid of the dynamic brakes, to stop the
train safely under all operating conditions.
CSXT Postaccident Actions
On February 2, 2000, the CSXT general manager for the Allegheny Division
issued Western District General Bulletin No. 207, SUBJECT: Mountain Subdivision
Timetable Special Instruction Modifications, which was effective immediately. For
eastbound trains between Altamont and West Virginia Central Junction (MP 207.8), the
maximum authorized speed for all trains was lowered from 25 to 20 mph. Engineers were
instructed: “If train speed cannot be maintained at or below the maximum authorized
speed of 20 mph, the train must be stopped immediately with an emergency brake
application.” Locomotives for all trains originating in Grafton were required to have a
running dynamic brake test before being attached to the train. Engineers of run-through
trains
47
were required to test the dynamic brakes before passing Westerman (MP 274).
Engineers of trains originating east of Westerman were required to make a running
dynamic brake test at the first available location before Mountain Lake Park (MP 229.8).
Detailed instructions were also given on how to perform the dynamic brake testing on one
or more locomotive units.
45
The FRA also indirectly controls maximum authorized speeds through track regulations, 49 CFR
Part 213, “Track Safety Standards,” which set maximum train speeds for different classes and conditions of
track.
46
Handbrakes can stop a train but currently cannot be operated from the locomotive cab. Dynamic
brakes can slow a train but cannot reliably stop a train under all operating conditions.
47
A run-through train does not originate in Grafton but stops there only for a crew change.
25 Railroad Accident Report
Analysis
Exclusions
Weather
Investigators considered whether the weather might have played a role in the
accident. Snow and ice could have accumulated between the brake shoes and wheels on
the coal cars and made the tread braking less effective, thus increasing the chance of
creating a runaway.
Postaccident examination of the running gear of the cars showed no signs of any
precipitation accumulation. The shallowness of the snow below the top of the rail and its
water content, as described by train and yard personnel and later verified at the accident
scene by investigators, did not support any scenario involving snow and ice accumulation
on the brake shoes or wheels. The fact that the train brakes had been applied much longer
than necessary to clean any snow and ice from the brake shoes before the descent of the
train down 17-mile grade also did not support the idea of a runaway caused by moisture
accumulation. Finally, the weather reports from the surrounding area recorded
temperatures slightly above or below freezing, again suggesting it was unlikely that there
had been an accumulation of blowing snow about the trucks and brake shoes of the freight
cars or locomotive. Consequently, the Safety Board concludes that the weather did not
cause or contribute to the accident.
Fatigue
Investigators reviewed the work/rest cycle records of the engineer and conductor,
their 72-hour histories before the accident, and the train handling data recorded by the
event recorder.
48
All parties to the investigation agreed that the crewmembers were
qualified to perform their duties according to CSXT procedures and accepted practice.
Nothing suggested that the train crewmen were fatigued or asleep. The crewmembers said
that they were rested in accordance with the Federal Hours of Service Act, and no
postaccident evidence or witness suggested anything to the contrary. The engineers work
schedule, his statement that he felt well rested, and the train handling data from the event
recorder all suggested that fatigue was not an element in this accident. Therefore, the
Safety Board concludes that crewmember fatigue was not a factor in the accident.
Toxicology
The engineer and conductor were tested after the accident, and no alcohol or drugs
were found. Therefore, the Safety Board concludes that neither alcohol nor drug use
caused or contributed to the accident.
48
The event recorder, by documenting each throttle and brake manipulation, provides some indication
of the operators level of alertness and skill.
Analysis 26 Railroad Accident Report
Track and Signals
The postaccident track inspections and a review of the maintenance-of-way
records revealed no contributory track anomalies. The 10 rail lubricators in the accident
area were inspected and found to function as designed, with no excessive lubricant found
that would have affected train braking. Nothing was found to suggest that either the track
conditions or the signal and train control systems caused or contributed to the accident.
The Safety Board concludes that neither the signal and train control systems nor the track
conditions were factors in the accident.
Event Recorder
Even though CSXT downloaded the three locomotive unit event recorders without
Safety Board or FRA supervision or permission, there was no evidence that the event
recorder data had been altered or tampered with.
Air Brake System
Postaccident testing of the train’s air brake system was not possible because so
many cars were destroyed in the accident; however, the air brake test performed on the
coal cars before they left the mine, the preaccident initial terminal air brake test, and the
set-and-release tests done when the helper locomotive was attached and when it was
detached suggest that the air brake system functioned as designed. The engineer stated that
the air brakes functioned “normally” and indicated that he had had no air brake problems
before the accident. The brake pipe pressure that was recorded on the event recorder from
both the front and rear of the train show that the air brake system had responded to the
engineer and had functioned as designed.
Postaccident examination of the coal car wheels and brake shoes, particularly
those at the end of the train, showed that the brakes had been applied heavily and for a
relatively long time. Many wheels showed discoloration caused by high heat, including
bluing on the tread and rim and red coloration on the wheel plate. The brake shoes were
burnt, glazed, and cracked and in various stages of degradation caused by the high heat.
The physical evidence on the wheels and brake shoes also showed that the applications
had propagated through the entire train without any train line blockage.
The conductor said that the EOT display in the locomotive cab showed 0 psi brake
pipe pressure after the engineer made the emergency brake application, also indicating
that the application had propagated to the end of the train without blockage. Investigators
concluded that the air brakes had functioned as designed and that the brake applications
had applied throughout the train. Therefore, the Safety Board concludes that the train’s air
braking system did not cause or contribute to the accident.
Analysis 27 Railroad Accident Report
Dynamic Braking and Train Speed
To a large extent, train speeds and train handling are determined empirically within
the limitations of the track structure and signal or train control systems. As with the
maximum authorized speed through the accident area, most speed limits have not changed
over a long period, particularly speed limits for common trains like coal trains, even
though the weight of trains has steadily increased over time. CSXT has been able to
maintain relatively high speeds despite increasing train weight because of the emphasis on
and continued improvement of locomotive dynamic braking.
Dynamic braking on the two trailing locomotive units, while available, could not
be activated because of the defective multiple-unit cable between the first and second
locomotive units. Because he did not have the benefit of full dynamic braking, the
engineer had to increase the air brake application beyond what normally would have been
expected in order to control speed. By so doing, he unwittingly overheated the tread-brake
system. Further, the maximum authorized speed for the accident grade had been
established based on the assumed availability and use of dynamic braking. Judging from
the CSXT’s experience of successfully negotiating 17-mile grade at the maximum
authorized speed, the combination of dynamic and air braking was, in fact, adequate to
hold a train at or under the established maximum authorized speed as the train progressed
down the grade. The Safety Board concludes that if all the available dynamic braking
could have been activated on the accident train, the derailment probably would not have
occurred.
Unfortunately, problems can occur when, as in this accident, the dynamic braking
system functions only partially or suddenly and unexpectedly fails when the train is
moving too fast to be stopped by the air brakes alone. Calculations and dynamometer
testing confirmed that CSXT eastbound loaded coal trains on 17-mile grade could not be
controlled or stopped at the maximum authorized speed without the use of significant
dynamic braking. The Safety Board concludes that by using the effects of dynamic
braking in its speed calculations, CSXT established a maximum authorized speed over and
down 17-mile grade that was too high to ensure that heavily loaded trains could be
stopped using air brakes alone.
The lead locomotive unit had no device for checking the real-time condition of the
dynamic brakes on the trailing locomotive units (or the signal continuity through the
multiple-unit cable), nor was such a device required at the time of the accident. The
condition of the dynamic brakes on trailing units can be determined by observing the
ampere gage in the cab of each of the trailing units, but those units normally do not have
crewmembers aboard. In this accident, an inexperienced trainman trainee was on board
the second unit, but only because of his aversion to cigarette smoke. And no one would
have been able to check the gage in the third unit because CSXT rules, for safety reasons,
generally prohibit crewmembers from moving between locomotive units while the train is
in motion. In short, even though CSXT had made the availability of dynamic brakes
critical by using their effects in calculating the maximum authorized speed, the company
had no requirement that the dynamic braking system be tested before or during use to
Analysis 28 Railroad Accident Report
determine how well it was functioning. After the accident, CSXT instituted a running
dynamic brake test procedure for its Mountain Subdivision.
As a result of the previously mentioned Safety Board investigation of the runaway
and subsequent derailment of a Southern Pacific Transportation Company train in San
Bernardino, California, in 1989, the Safety Board issued the following recommendation to
the FRA regarding dynamic braking:
R-90-23
Study, in conjunction with Association of American Railroads, the feasibility of
developing a positive method to indicate to the operating engineer in the cab of
the controlling locomotive unit the condition of the dynamic brakes on all units in
the train.
The Safety Board classified this recommendation “ClosedUnacceptable
Action/Superseded” after its investigation of a runaway Union Pacific train at Kelso,
California.
49
After that accident, the Safety Board issued the following safety
recommendation to the FRA:
R-98-6
Require railroads to ensure that all locomotives with dynamic braking be
equipped with a device in the cab of the controlling locomotive unit to indicate to
the operating engineer the real-time condition of the dynamic brakes on each
trailing unit.
This recommendation was classified “OpenAcceptable Response” on
January 11, 2000.
The FRA has included in the new power brake regulations (49 CFR 232.109) the
following dynamic braking requirements:
(a) A locomotive engineer shall be informed in writing of the operational status of
the dynamic brakes on all locomotive units in the consist at the initial terminal or
point of origin for a train and at other locations where a locomotive engineer first
takes charge of a train.
(g) All locomotives equipped with dynamic brakes and ordered on or after August
1, 2002, or placed in service for the first time on or after April 1, 2004, shall be
designed to:
(1) Test the electrical integrity of the dynamic brake at rest; and
(2) Display the available total train dynamic brake retarding force at vari-
ous speed increments in the cab of the controlling (lead) locomotive.
49
National Transportation Safety Board, Derailment of Union Pacific Railroad Unit Freight Train
6205 West Near Kelso, California, January 12, 1997, Railroad Accident Report NTSB/RAR-98-01
(Washington, D.C.: NTSB, 1998).
Analysis 29 Railroad Accident Report
(h) All rebuilt locomotives equipped with dynamic brakes and placed in service on
or after April 1, 2004, shall be designed to:
(1) Test the electrical integrity of the dynamic brake at rest; and
(2) Display either the train deceleration rate or the available total train
dynamic brake retarding force at various speed increments in the cab of the
controlling (lead) locomotive.
While the new regulation does not require a dynamic braking display for each
trailing locomotive unit, as recommended by the Safety Board, a total real-time dynamic
braking effort display as described above may be as useful and acceptable. The Safety
Board is also pleased to note that the accelerometer will be used in conjunction with the
FRA regulation that will require a train descending a grade of 1 percent or greater to be
immediately stopped if it exceeds the maximum authorized speed by more than 5 mph.
Therefore, the Board has reclassified Safety Recommendation R-98-6
“ClosedAcceptable Alternate Action.”
Tread Brakes/Air Brakes and Stopping Ability
High-friction composition-type brake shoes such as those involved in the
Bloomington accident significantly degrade when the average wheel temperature exceeds
500° F. Considerable “heat” or brake fade also occurs around these higher temperatures,
which results in a noticeable drop in the coefficient of friction and braking ability.
At the time of the accident, the maximum authorized speed from Swanton (MP
219.4) to Bloomington (MP 206.2) was 25 mph. CSXT lowered the maximum authorized
speed to 20 mph after the accident in an attempt to create a safe speed. CSXT Rule 34-D
requires that, on descending grades of 1 percent or more, a train must be stopped using an
emergency brake application if the train’s speed reaches 5 mph more than the maximum
speed permitted for that train. Thus, even under the reduced postaccident maximum speed
of 20 mph, the engineer could still attain 25 mph before attempting to stop the train. For
the accident train, at 20 mph, the recognized safe bhp of 30 would have been exceeded by
more than 10 percent, and at 25 mph, the bhp would have been exceeded by more than 62
percent.
According to commonly accepted air brake industry standards, a train with cars
that have 36-inch diameter wheels, such as the accident train, should not exceed an
average bhp of 30. The accident train had such a bhp, but only when it was traveling about
15 mph. At 20 mph, its bhp was 49.54; and at 30 mph, its bhp was 64.40. The large
disparity in bhp between the recommended 30 and the actual number the accident train
had at its maximum authorized speed translates into significant increases in the heat
generated at the interface between the brake shoe and wheel tread. The increases in heat,
in turn, degrade the brake shoes and cause heat fade and the loss of molecular adhesion,
resulting in a catastrophic loss of retardation and braking powera runaway train.
Analysis 30 Railroad Accident Report
Actual brake shoe force measurements were taken for each brake application on
identical coal cars on August 8, 2000. Using these shoe forces, the bhp calculations were
then substantiated by dynamometer tests performed on August 22, 2000. These test results
also indicated that the heat from the applied accident train brakes had reached the critical
point about the time the train began to pass through Swanton Flats, MP 219.4, only about
3.6 miles into 17-mile grade. By that time, the temperature of the brake shoes/wheels
exceeded the thermal limit of the brake shoes and resulted in a loss of braking power.
The dynamometer tests validated the theoretical calculations. The calculations and
dynamometer tests showed that the maximum authorized speed of 25 mph was too high
and that, in fact, any speed above 15 mph was too high to allow the train to be brought to a
stop by the air brakes alone. Because the air brake system is the only braking system
capable of bringing a train to a stop, it is incumbent upon railroads to set maximum speeds
that ensure that trains can be stopped without the use of supplemental braking.
50
At the
time of the accident, there was no regulation requiring a train to have the capability to stop
by use of the air brake system alone. According to FRA officials, the agency believed this
was understood by the railroads, but it was not. CSXT management had included the
effect of dynamic braking in determining maximum authorized speeds. Including in the
maximum speed calculation the effects of dynamic brakes, which cannot be relied upon to
stop the train, resulted in speeds that violated the spirit of the “primary brake” and
prevented the engineer from stopping the accident train with the air brakes alone.
51
The
maximum authorized speed down 17-mile grade should probably have been no greater
than 15 mph to ensure safe operation in the event of either partial or full dynamic brake
failure or an unintended release of the air brake.
CSXT does actively update its train handling practices as train equipment
improves. To a large extent, it does the updating by using computer simulators, such as a
train dynamics analyzer. The analyzer is used to match methods of train handling with
current and proposed maximum authorized speeds; however, no software is yet capable of
replicating the loss of braking caused by heat fade. (Such software is under development.)
Since a train dynamics analyzer cannot replicate heat fade, a simulator may indicate that a
train can be stopped when, in reality, it may be unstoppable. Running an actual train on
steep grades and applying the brakes until heat fade occurs is dangerous and expensive
and is therefore not practical. The most available current methods of determining the
maximum authorized speed are by calculation or by using dynamometers; however, most
railroads use neither.
As already noted, the Safety Board has previously investigated runaway train
accidents at San Bernardino and Kelso, California, involving the Southern Pacific and the
Union Pacific Railroads. There have been similar incidents on the BNSF Railway on
Cajon Pass. All these accidents and incidents involved, as does the Bloomington accident,
the dependence on and sudden loss of dynamic braking. The Safety Board is concerned
50
Unlike automobiles, a train can attain speeds, particularly when traveling downgrade, that exceed the
capacity of the brakes to bring it to a stop.
51
At the time of this report, the FRA had not cited CSXT for any rule violation regarding the maximum
authorized speed in this accident.
Analysis 31 Railroad Accident Report
that maximum authorized speeds enabling a train to stop by the air brake system alone are
not, and have not been, audited or re-evaluated by the major carriers as frequently as
necessary over time as trains have become heavier and braking systems have changed.
Therefore, the Safety Board believes that the class I railroads should calculate steep-grade
maximum authorized speeds to ensure that trains can be stopped by use of the air brake
system alone. The Safety Board also believes all class I railroads should establish
procedures to revise maximum authorized speeds as necessary.
CSXT Management Oversight
Given the circumstances at the time of the accident, including the maximum
authorized speed and the absence of a method to warn the engineer that he did not have
access to full dynamic braking, the engineers actions did not cause or contribute to the
accident. Without the added retardation afforded by full dynamic braking and given the
magnitude of the difference in energy
52
between what was developed during the
investigation as a maximum safe speed of 15 mph and the maximum authorized speed of
25, it is doubtful whether the engineer could have stopped the train regardless of what he
did.
According to the dynamometer tests, the “point of no return” was around Swanton
Flats, MP 219.4, only 3.6 miles down 17-mile grade, a point long before an engineer
would normally be concerned about controlling or stopping the train. In fact, the engineer
was concerned about stalling rather than stopping the train. Consequently, he powered
against the brakes. The event recorder showed that the train’s speed from MP 223 to MP
217.22 never exceeded the maximum authorized 25 mph; and yet, as confirmed by the
dynamometer tests, the train became uncontrollable. The difference in energy is even
greater at 30 mph, which was still within the allowable +5 mph margin of the operating
rules at the time. Therefore, the Safety Board concludes that no matter what actions the
engineer took, he probably could not have prevented a runaway because of the speed at
which he was authorized to operate and the condition of the dynamic brakes.
Engineer’s Actions
While the engineers actions do not appear to have directly caused or contributed
to the accident, some of his actions, or some of his failures to act, reflect upon the efficacy
of his supervision, training, and support.
The engineer had more than 29 years of railroad experience at the time of the
accident. He was well regarded by railroad management and coworkers as a “senior”
engineer. He had been in engine service since 1976 and had made numerous runs along the
Grafton to Cumberland route. He had come back to road service on January 9, 2000, a few
weeks before the accident. He had just had his last rules class and test 3 days before the
accident. He had completed 2 days of recertification
53
training (49 CFR Part 240) at the
CSXT Training Center, Cumberland, Maryland, on May 4, 1999, which consisted of
52
Energy as measured in bhp.
53
Recertification is not the same as requalification.
Analysis 32 Railroad Accident Report
classroom presentations and tests. And yet, in this accident, the engineers train handling
was not optimal.
Situational Awareness. According to FRA inspectors, CSXT operating officers,
and CSXT engineers with knowledge of and experience with 17-mile grade, it is possible
to control a loaded coal train headed by three modern locomotive units with a 12-pound or
less brake pipe reduction and light throttle or dynamic brake modulation. Earlier in the
trip, the helper engineer had noted that the train engineer had used more air brake than was
normal or routine. The accident engineer stated several times that he attributed his use of
more air brake than usual to the wet snow and icy rail; however, his need to power against
a 17-pound reduction with up to a 6th notch of throttle belies this contention.
The engineer said he was afraid that the train would stall at Swanton Flats if he did
not power against the brakes. Thus, he should have realized that the brakes were effective
and not affected at that time by snow or ice. An engineer who was fully situationally
aware and who understood the grade and the newer locomotives would likely have been
aware that something was wrong long before the point where the train could not be
controlled with customary train handling.
Powering Against the Brakes. As mentioned earlier, CSXT rules state, “When
necessary to apply power descending long heavy grades, trains must not be pulled
54
for a
distance greater than 2 miles if the brake pipe reduction is 18 pounds [psi] or greater.”
According to the event recorder, the engineer had steadily increased the air brake
application for more than 10 minutes, until he had a 17-pound reduction of the brake
pipe
55
at MP 220.12 (Swanton) at a speed of 24 mph. He maintained the 17-pound
reduction for the next 9 minutes at a speed of 24 mph. It is significant that he powered
against this 17-pound reduction through Swanton for about 5 minutes and 2 miles, at one
point reaching the 6th notch on the throttle. He further reduced the brake pipe to 18
pounds at MP 216.46 at a speed of 28 mph.
Thus the engineer had been operating at the limit or just short of the 18-pound
limit, and the brakes had probably already reached the thermal point of no return at the
speed the train was moving. He continued to make progressive 1-pound reductions for
about the next 4 minutes as the speed of the train increased to 34 mph, when he finally
placed the brakes in emergency. Had the engineer gone into emergency shortly after
reaching the 18-pound reduction, as required by rule, he probably would not have been
able to stop, since the train’s brakes were probably already beyond the critical thermal
limit.
The actions of the engineer, and the effects of those actions, point out a problem
with the CSXT “18-pound” rule. As written, the rule is inadequate to ensure that an
54
In order for the train to be pulled regardless of whether the train brakes are applied, the locomotives
must be in the power mode.
55
The brake pipe pressure is 90 psi minus the total reduction. In this case a 17-pound reduction will
result in a brake pipe pressure of 73 psi.
Analysis 33 Railroad Accident Report
engineer does not, as the accident engineer did, power against his brakes at a speed that is
likely to cause excessive heat generation and loss of control. All the calculations for bhp
are based on the factor of speed or velocitythe greater the speed, the greater the bhp and
heat energy generated by the friction brakes. The CSXT rule does not include a critical
limit for speed. The Safety Board concludes that, because the CSXT rule regarding
powering against the brakes does not address train speed, it is inadequate to ensure that an
engineer does not exceed the bhp and heat energy limitations of the tread brake system and
thereby create conditions that can lead to a runaway train.
Therefore, the Safety Board believes that CSXT should modify CSXT Rule 3.3.7,
Speed Control on Descending Grade, Paragraph C, “Use of Power on Heavy Descending
Grades,” to impose a speed limit in addition to the maximum distance and brake pipe
reduction currently imposed to prevent excessive heat generation, heat fade, and loss of
braking ability.
Engineer’s Support and Training
The Safety Board examined the management and supervisory support the engineer
received as well as and engineers actions during the accident. The Safety Board also
examined the effect that the CSXT locomotive engineer training and the recertification
program might have had on those actions. Since the engineer had become an engineer in
1976, his most recent training was considered.
The engineer said that he had transferred from a yard to a road assignment only a
few weeks before the derailment. Consequently, the general road foreman told the
engineer that he could have a pilot for two roundtrips. For the engineers first trip on the
assignment, a pilot was provided for the westbound leg, from Cumberland to Grafton
(uphill, in the opposite direction of the accident train). Because the crew returned to
Cumberland by taxi, the engineer did not make an eastbound trip (which would have taken
him down 17-mile grade) with the pilot.
The engineer said that when he was called for his second trip, he asked that a pilot
accompany him on the return to Cumberland. But, he said, a crew caller told him that the
crew caller and the lead crew caller would decide whether the engineer needed a pilot and,
if so, would provide one. No pilot was provided.
Additionally, according to the engineer and to CSXT records, no supervisor had
ridden with the engineer while he operated a train down 17-mile grade to monitor his
performance or to provide specific train handling instruction and guidance, even though
this area was a critical train handling portion of the railroad. And while the engineer had
made one trip down the grade as an observer and had operated a train on eight trips down
17-mile grade in the weeks preceding the accident (most of them with loaded coal trains),
neither he nor his supervisors could know for certain whether his train handling technique
was appropriate or whether it offered some safety margin in case of an unforeseen event.
Analysis 34 Railroad Accident Report
Use of End-of-Train Emergency Switch
After the engineer placed the train brakes in emergency with the automatic brake
handle, he did not confirm that the emergency application had propagated to the end of the
train until a minute and a half later when he saw the head-end display showing 0 psi
pressure for the train’s EOT. Had he activated the EOT emergency brake application
switch immediately after initiating the emergency application, he would have ensured that
the emergency application had reached the end of the train.
Immediately throwing the EOT switch not only propagates the brake application
more rapidly because the release of air pressure comes from both ends of the train rather
than just the head end, but it also ensures full propagation even if a kink or other
obstruction is blocking the train line. Thus, the prudent action would have been to
immediately flip the EOT emergency brake switch. The needless time taken to confirm
that the emergency propagation was complete could, under some circumstances, have
been critical. In this case, because the engineer had already exceeded the thermal limit of
the brakes by the time he placed the brakes in emergency, his failure to immediately
initiate an EOT emergency application became moot.
The engineer said he had been trained to use the two-way EOT emergency switch
only if the EOT was not showing 0 psi after an emergency brake application. Since using
the switch causes no damage to any equipment on the train while offering the advantages
of a quicker and more thorough response, the Safety Board fails to see the benefit in
restricting its use to what is, in effect, a backup system. CSXT agrees and has an automatic
two-way emergency EOT switch on all new locomotives. In addition, CSXT offers
instruction in the use of the switch in its engineer classes and, in its operating rules,
requires immediate use of the switch in an emergency.
Emergency Radio Use
During the runaway, the train crew was unable to contact the dispatcher but was
able to contact the railroad operator at West Keyser, Virginia, as the train passed Bond at
MP 212.6. The engineer attributed his inability to contact the dispatcher to the fact that the
radio on the ex-Conrail lead locomotive was different from the radios found on the CSXT
locomotives that he more commonly operated. Postaccident testing of the engineers radio
and subsequent investigation revealed that the radio worked as designed.
U.S. railroads use five basic styles of locomotive radios, each of which is
compatible with the others, regardless of railroad. Except for superficial details such as
dials, touch pads, and channel display, all railroad radios are similar; that is, they use the
same frequencies or channels. Timetable instructions list the particular channels for
emergency use and/or for calls to the dispatcher. Had the engineer properly set the channel
for the dispatcher and then pushed the correct keypad numbereither “9” for emergency
or “5” for the dispatcherhe would have reached the dispatcher.
The Safety Board concludes that CSXT failed to train and oversee the engineer
sufficiently and effectively, as evidenced by (1) management’s failure to provide the
engineer with a pilot when requested, (2) management’s failure to fully evaluate the
Analysis 35 Railroad Accident Report
engineer over the critical portion of the railroad where the accident took place, (3) the
engineers failure to use the EOT emergency brake switch, (4) the engineers imprudent
use of power during brake application, and (5) the engineers reported inability to use the
radio to contact the dispatcher. Therefore, the Safety Board believes that CSXT
management should systematically ensure that engineers are provided with pilots, as
appropriate, and that locomotive engineers are fully evaluated over the whole of their
territories, particularly in critical areas of train handling such as steep grades.
The Safety Board also believes that CSXT should revise its locomotive engineer
training and requalification programs as necessary to ensure that they address (1) the
emergency use of the two-way EOT emergency switch, (2) the proper use of power during
a brake application to prevent heat fade and loss of braking, and (3) the use of all styles of
locomotive radios, especially their use during emergency situations to call the dispatcher.
36 Railroad Accident Report
Conclusions
Findings
1. There was no evidence that the following factors were causal or contributory to the
accident: the weather; crewmember fatigue, or alcohol or drug use of any kind.
2. Neither the signal and train control systems nor the track conditions were factors in
the accident.
3. The train’s air braking system did not cause or contribute to the accident.
4. By using the effects of dynamic braking in its speed calculations, CSX Transportation
established a maximum authorized speed over and down 17-mile grade that was too
high to ensure that heavily loaded trains could be stopped using air brakes alone.
5. No matter what actions the engineer took, he probably could not have prevented a
runaway because of the speed at which he was authorized to operate and the condition
of the dynamic brakes.
6. If all the available dynamic braking could have been activated on the accident train,
the derailment probably would not have occurred.
7. Because the CSX Transportation rule regarding powering against the brakes does not
address train speed, it is inadequate to ensure that an engineer does not exceed the
braking horsepower and heat energy limitations of the tread brake system and thereby
create conditions that can lead to a runaway train.
8. CSX Transportation management failed to train and oversee the engineer sufficiently
and effectively, as evidenced by (1) management’s failure to provide the engineer
with a pilot when requested, (2) managements failure to fully evaluate the engineer
over the critical portion of the railroad where the accident took place, (3) the
engineers failure to use the end-of-train emergency brake switch, (4) the engineers
imprudent use of power during brake application, and (5) the engineers reported
inability to use the radio to contact the dispatcher.
Probable Cause
The National Transportation Safety Board determines that the probable cause of
the January 30, 2000, derailment of CSX Transportation train V986-26 near Bloomington,
Maryland, was the railroad’s practice of including dynamic braking in determining
maximum authorized speed without providing the engineer with real-time information on
the status of the dynamic braking system.
37 Railroad Accident Report
Recommendations
As a result of its investigation of the January 30, 2000, derailment of CSXT train
V986-26 near Bloomington, Maryland, the National Transportation Safety Board makes
the following safety recommendations:
To CSX Transportation, Inc.:
Systematically ensure that engineers are provided with pilots as
appropriate and that locomotive engineers are fully evaluated over the
whole of their territories, particularly in critical areas of train handling such
as steep grades. (R-02-8)
Revise your locomotive engineer training and requalification programs as
necessary to ensure that they address (1) the emergency use of the two-way
end-of-train emergency switch, (2) the proper use of power during a brake
application to prevent heat fade and loss of braking, and (3) the use of all
styles of locomotive radios, especially their use during emergency
situations to call the dispatcher. (R-02-9)
Modify CSX Transportation Rule 3.3.7, Speed Control on Descending
Grade, Paragraph C, “Use of Power on Heavy Descending Grades,” to
impose a speed limit in addition to the maximum distance and brake pipe
reduction currently imposed to prevent excessive heat generation, heat
fade, and loss of braking ability. (R-0-10)
To all class I railroads:
Calculate and document steep-grade maximum authorized speeds to ensure
that trains can be stopped by use of the air brake system alone. (R-02-11)
Establish procedures to revise steep-grade maximum authorized speeds as
necessary. (R-02-12)
38 Railroad Accident Report
BY THE NATIONAL TRANSPORTATION SAFETY BOARD
MARION C. BLAKEY
Chairman
CAROL J. CARMODY
Vice Chairman
JOHN A. HAMMERSCHMIDT
Member
JOHN J. GOGLIA
Member
GEORGE W. BLACK, JR.
Member
Adopted: March 5, 2002
Recommendations
39 Railroad Accident Report
Appendix A
Investigation
The National Transportation Safety Board Communications Center was notified of
the derailment at Bloomington, Maryland, about 8 a.m. on January 30, 2000, and two
Safety Board investigators were launched to Bloomington, arriving on scene about 11:00
a.m. No Board Member went to the scene.
No public hearing was held on this accident. Testimony was taken in Grafton, West
Virginia, immediately after the accident on February 1, 2000. Follow-up testimony was
taken in Jacksonville, Florida, at CSXT headquarters on November 8, 2000, and in
Cumberland, Maryland, on November 28, 2000.
Load-cell brake shoe measurements were performed at the CSXT car shop in
Cumberland, Maryland, on August 8 and 9, 2000.
On August 22, 2000, representatives of parties to the accident gathered at the
Railroad Friction Products Corporation plant at Maxton (Laurinburg), North Carolina,
where a dynamometer machine tested brake shoes under the accident conditions.
this page intentionally left blank
41 Railroad Accident Report
Appendix B
How Freight Train Air Brakes Work
The air brake system on a train is designed to slow or stop a train through the use
of compressed air. The compressed air is used to push a piston within a cylinder. Usually,
through a series of rods and levers, the piston’s movement forces brake shoes against car
or locomotive wheels or discs to slow their rotation through friction. The air is compressed
by an air compressor in the locomotive and stored for use in the main reservoirs (large
tanks) on the locomotive. (See diagram that follows.)
The compressed air and the brakes are controlled by the engineer using an
automatic brake-valve handle on a locomotive control stand. The automatic brake valve
controls the train’s brakes (including the locomotive’s brakes) and has three functions: (1)
to apply the brakes, (2) to release the brakes, and (3) to charge or recharge the air brake
system. Another valve handle, called the independent brake valve, is used by the engineer
to independently control only the locomotive’s brakes.
Figure 1. Brake Diagram
Appendix B 42 Railroad Accident Report
Each railroad car has one or more brake-cylinder pistons, a reservoir (storage
tank), associated piping, and a control valve. The control valves on cars are designed to
respond to changes in air pressure in the train line. The train line is the physical connection
of the locomotive and the cars’ air brake systems through metal pipes and connecting
flexible air hoses at the ends of each railroad vehicle.
The air pressure within the train line is called the brake pipe. When brake pipe
pressure (in the train line) is reduced by the engineer, each cars control valve senses the
drop and applies the brakes by sending some air stored in the cars reservoir to its brake
cylinder(s). The amount of air sent to the air brake cylinder is proportional to the drop in
brake pipe pressure. Up to a point, the larger the drop in brake pipe pressure, the more air
the control valve sends from the reservoir to the brake cylinder and the greater the amount
of braking force created.
To release the brakes, the engineer lets more air into the train line from the
locomotive main reservoirs, increasing the brake pipe pressure. Each cars control valve
senses this increase in air pressure and exhausts air from the brake cylinder, releasing the
brakes. A return spring within the brake cylinder pushes the piston back into the cylinder,
and the brake shoe backs away from the wheel or disc. At the same time, the cars control
valve takes some air from the train line to replenish any air that the cars braking system
has used from its reservoir to charge or recharge its system.
The brake-pipe pressure is determined by the engineer, who turns a knob that sets
the regulating or feed valve. The regulating valve reduces the pressurized air from the
main reservoir to a determined amount for delivery to the equalizing reservoir, which then
dictates brake pipe pressure. The equalizing reservoir is a small reference volume used to
control the much larger brake pipe or train line volume. The equalizing reservoir allows
the engineer to make immediate predetermined changes to the brake-pipe pressure without
having to wait for the changes to take place in the train and stabilize.
Since the train line connections through and between cars are not perfect, some of
the compressed air leaks out of the system. In order to prevent the car control valves from
sensing a drop in air pressure from leakage and inadvertently applying the brakes, the
automatic brake valve in the engineers locomotive control stand has a maintaining
feature. The maintaining feature automatically sends just the right amount of air into the
brake pipe, regardless of whether the brakes are applied or released, to make up for any
train line system leakage.
Since the maintaining feature is located in the locomotive, there is usually a
constant flow of air toward the rear of the train. Train line leakage progressively draws off
air from the brake pipe as it travels toward the rear of the train, dropping air pressure. This
gradual drop in brake pipe pressure is called gradient, and represents the difference in
brake pipe pressure between the front of the train and the rear of the train.